Failure analysis of an A333Gr6 pipeline after exposure to a hydrogen sulfide environment

2013 
Abstract The analysis of an A333Gr6 pipeline failure was conducted after exposure to high H 2 S partial pressure for several hours. Chemical composition, metallurgical structure, steel pipe hardness, and the welding joint near the broken position were studied. The chemical compositions of corrosion products inside the steel pipe were also analyzed. Results show that corrosion products consist of Fe 3 O 4 and FeOOH without ferrous sulfide. Stress analysis was obtained through the finite element analysis method. The failure analysis and calculation results show that spontaneous ferrous sulfide combustion in a high H 2 S environment leads to high temperature and pressure in the pipe, resulting in pipeline breakage.
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