JV Task - 129 Advanced Conversion Test - Bulgarian Lignite
2009
The objectives of this Energy & Environmental Research Center (EERC) project were to evaluate Bulgarian lignite performance under both fluid-bed combustion and gasification conditions and provide a recommendation as to which technology would be the most technically feasible for the particular feedstock and also identify any potential operating issues (such as bed agglomeration, etc.) that may limit the applicability of a potential coal conversion technology. Gasification tests were run at the EERC in the 100-400-kg/hr transport reactor development unit (TRDU) on a 50-tonne sample of lignite supplied by the Bulgarian Lignite Power Project. The quality of the test sample was inferior to any coal previously tested in this unit, containing 50% ash at 26.7% moisture and having a higher heating value of 5043 kJ/kg after partial drying in preparation for testing. The tentative conclusion reached on the basis of tests in the TRDU is that oxygen-blown gasification of this high-ash Bulgarian lignite sample using the Kellogg, Brown, and Root (KBR) transport gasifier technology would not provide a syngas suitable for directly firing a gas turbine. After correcting for test conditions specific to the pilot-scale TRDU, including an unavoidably high heat loss and nitrogen dilution by transport air, the best-case heatingmore » value for oxygen-blown operation was estimated to be 3316 kJ/m{sup 3} for a commercial KRB transport gasifier. This heating value is about 80% of the minimum required for firing a gas turbine. Removing 50% of the carbon dioxide from the syngas would increase the heating value to 4583 kJ/m{sup 3}, i.e., to about 110% of the minimum requirement, and 95% removal would provide a heating value of 7080 kJ/m{sup 3}. Supplemental firing of natural gas would also allow the integrated gasification combined cycle (IGCC) technology to be utilized without having to remove CO{sub 2}. If removal of all nitrogen from the input gas streams such as the coal transport air were achieved, a heating value very close to that needed to fire a gas turbine would be achieved; however, some operational issues associated with utilizing recycled syngas or carbon dioxide as the transport gas would also have to be resolved. Use of a coal with a quality similar to the core samples provided earlier in the test program would also improve the gasifier performance. Low cold-gas efficiencies on the order of 20% calculated for oxygen-blown tests resulted in part from specific difficulties experienced in trying to operate the pilot-scale TRDU on this very high-ash lignite. These low levels of efficiency are not believed to be representative of what could be achieved in a commercial KRB transport gasifier. Combustion tests were also performed in the EERC's circulating fluidized-bed combustor (CFBC) to evaluate this alternative technology for use of this fuel. It was demonstrated that this fuel does have sufficient heating value to sustain combustion, even without coal drying; however, it will be challenging to economically extract sufficient energy for the generation of steam for electrical generation. The boiler efficiency for the dried coal was 73.5% at 85% sulfur capture (21.4% moisture) compared to 55.3% at 85% sulfur capture (40% moisture). Improved boiler efficiencies for this coal will be possible operating a system more specifically designed to maximize heat extraction from the ash streams for this high-ash fuel. Drying of the coal to approximately 25% moisture probably would be recommended for either power system. Fuel moisture also has a large impact on fuel feedability. Pressurized gasifiers generally like drier fuels than systems operating at ambient pressures. The commercially recommended feedstock moisture for a pressurized transport reactor gasifier is 25% moisture. Maximum moisture content for a CFB system could be approximately 40% moisture as has been demonstrated on the Alstom CFB operating on Mississippi lignite. A preliminary economic evaluation for CO{sub 2} was performed on the alternatives of (1) precombustion separation of CO{sub 2} in an IGCC using the KBR transport gasifier and (2) postcombustion CO{sub 2} capture using a CFBC. It appears that the capture of CO{sub 2} from the high-pressure IGCC precombustion system would be less costly than from the low-pressure postcombustion CFBC system by a factor of 1.5, although the cost difference is not directly comparable because of the model input being limited to a higher coal quality than the Bulgarian lignite. While the decision to pursue precombustion removal of carbon dioxide has been technically proven with the Rectisol{reg_sign} and Selexol{trademark} processes, General Electric and Siemens have not sold any gas turbine systems running on the high-hydrogen syngas. They have successfully demonstrated a gas turbine on syngases containing up to 95% hydrogen. The technological hurdles should not be too difficult given this experience in the gas turbine industry.« less
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